Sunday, 18 November 2012

Maintenance in Montreal part 2


Doing maintenance isn’t quite as glamorous as travelling across the country by train, so the short story of the last couple weeks is that the DGRMS, a system which pushes a set of wheels laterally against the rail, was out for maintenance. It came back with more problems than it left with, a support bar broken off, grease lines not connected, vertical displacement measurements outputting wrong signals, software update bugs, etc. After lots of work (18 days) in montreal, we finally did a shakedown, where we go for a trip and test the software, and it all works. So we are leaving on Monday, heading west, and if there are no more problems we should be going all the way to Vancouver, which means a trip through the rockies!!

The longer story: (continued from the previous blog entry)
After finally getting a day off on Sunday (oct 28th), we got back to work on the train on Monday. We got kicked out of the shop late on Tuesday, so we parked nearby and powered up the generators, and the GRMS moved as it should. Unfortunately, some of the sensors weren’t displaying proper readings. I worked for 4 hours to connect a 6-pin cord to its appropriate plug, which was located in a spot where you could fit either a mirror, or a flashlight, or a hand, but not all three at the same time. Once it was finally connected, we moved the axle around to see what the readings were, and the vertical displacements were completely wrong. After significant troubleshooting and finally calling the manufacturer of the hydraulic cylinders, we discovered that for some reason unknown to everyone, a different sort of displacement transducer was used, and the signal output was no longer being transformed properly. As replacing the cylinder would have taken about a week, and re-wiring and writing a new transformation software would also take about a week, we decided to order separate vertical displacement measurements and attach them on the side of the DGRMS, as was done previously.

This was decided Thursday, and during the afternoon I found out that it was cheaper to fly me home to Waterloo over the long weekend (CP takes remembrance day off) than pay for hotel/meals. The flight was 550, and the hotel was 150 a night, which that just by itself was cheaper. So I booked a flight for Friday morning to Toronto, and bused up to waterloo. Hung out at grebel for a bit, went rock climbing with my brother and some people from church, went to a worship service with a good friend, played an awesome game of ultimate (during which I found out that sitting for 2 months really takes a toll on your fitness),  and hung out with family. Left late Monday, and got back to work on Tuesday.

The 2-inch support rod that was broken off in transit had finally arrived, so that was installed Tuesday morning. We were still waiting for the vertical displacement measurement devices, so we finished up smaller tasks, tied up all the grease lines, replaced some light bulbs, refilled water, and tried to keep busy. That afternoon a shipment arrived from the manufacturer of the cylinders, and the contained transformers for the vertical displacement! We connected it to the left cylinder, and the readings showed correct values! That was a great turn of events. So we started making a box to secure the transformers to the car. Everything we do has to be tied down and connected as securely as possible, as the train shakes around all day long. For the rest of the day, and Wednesday, we updated the joint bar detection software. After noticing a lot of bugs and getting multiple updates, we got a crew late Wednesday to run us around a bit. We put pieces of tape on some joint bars, numbered them 1 to 25, and ran over them a bunch of times. The software took a picture of every single one, which was a large improvement over the previous system, which would miss some joints.

Thursday we hooked up the vertical displacement cylinders and prepared for a final calibration, only to discover that the right cylinder wasn’t working. After troubleshooting all we could, we determined that the only possible explanation was that the transducer inside the cylinder itself was malfunctioning. After a couple calls to the higher-ups, we decided that we could run on just one measuring vertical displacement, as the chance of only one wheel derailing is pretty slim. We then calibrated the whole system, and the numbers were close to what it was originally set as, which was good news. Friday was finally a shakedown, we got a crew to take us to a 20 mile stretch of main track, and we tried forward and backwards, increasing and decreasing mileposts, and checked every possible scenario of what we would be doing while testing. After fixing a couple bugs, the system finally works well. We took a break for lunch to eat out at a restaurant, and noticed a significant number of people walking around. We realized that it was 4:30pm, and that that was the time that regular people end work. And yet we were going out for lunch after starting at 7:00am. But the system finally works!

We had done a lot of work that week, so all day Saturday was spent gloriously doing nothing, mostly lying in my bed watching a movie or a Barcelona game on my computer. I ventured outside for lunch, and stumbled across a santa clause parade, which I watched for a while. Sunday morning was also resting, and in the afternoon Anthony and I went shopping and cleaned up the train. The fridge was pretty empty, and the total grocery bill was close to $1500 (we did several trips).

The plan now is leaving Monday heading west, and if everything goes well and there are no breakdowns or more maintenance, then we should make it all the way to Vancouver, which means a trip through the rockies!! It’s been nice having someone clean up after me and make my bed each day (I’ve been staying in a hotel all this time), but I’m also really glad to be moving again. Looking forward to some new scenery!

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